View Single Post
Unread 13-01-2008, 11:10   #4
Mark Gleeson
Technical Officer
 
Mark Gleeson's Avatar
 
Join Date: Dec 2005
Location: Coach C, Seat 33
Posts: 12,669
Default

The cause of the derailment was a broken axle, which broke about 300m before the set of points, points just diverted the train more off the track

Most staff are quite decent, there are all the same a high number of bad apples in Irish Rail. The chaos on Friday was mainly as a result of poor management

IE really don't have any class of plan for these situation, no notice up in Pearse on Saturday about the situation for instance. Crew in Skerries, being old school have a rather worn blackboard which they can quickly place a notice. London Underground have equipped every station with a white board and markers, ultra low tech but very very effective

The Rail Incident Investigation Unit will certainly be doing an investigation. Looking at the situation it doesn't look like the Northbound track was actually physically blocked at any stage, the whole site was probably closed pending the Rail Incident Investigation Unit crew visiting and documenting the situation. IE then ran a test train through which fitted with only a few inches (instead of the usual foot plus gap). IE had nothing on site to move a 75 ton wagon

Would a train going the opposite direction have struck the derailed train? doubtful.

Last edited by Mark Gleeson : 13-01-2008 at 11:28.
Mark Gleeson is offline   Reply With Quote